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Description: Book cover
Coolant Waste Minimization Using a Coalescing Plate Separator
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Description: Book cover
Coolant Waste Minimization Using a Coalescing Plate Separator

Coolant Waste Minimization Using a Coalescing Plate Separator

Coolant Waste Minimization Using a Coalescing Plate Separator

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Description: Book cover
Coolant Waste Minimization Using a Coalescing Plate Separator
Abstract
During 1998 a project was initiated at Wolverine Tube in Shawnee, Oklahoma to increase machine tool coolant life and also to increase the life of the tooling used to manufacture copper tubing from copper billets.The coolant was becoming contaminated with tramp oil that provided a substrate for bacterial growth and tended to upset the operations of the tube reducer machine. The tramp oil also caused undue wear on the tooling and reduced tooling life.An initial test was conducted using a small, relatively low flow rate coalescing plate separator manufactured by Facet International, Inc. This test was very successful, but the flow rate from the test separator was not adequate for the requirements of the tube reducing operations. A larger separator was subsequently constructed and installed. The separator has been in service more than a year.The paper will present the results of the initial testing as well as the longer-term reduction in waste coolant production and tooling/operating cost reduction. Coolant waste is reduced to approximately 1/3 of previous quantities and costs are substantially reduced. The tramp oil removed by the separator is being recycled as well, and information on this recycling will be presented.
During 1998 a project was initiated at Wolverine Tube in Shawnee, Oklahoma to increase machine tool coolant life and also to increase the life of the tooling used to manufacture copper tubing from copper billets.The coolant was becoming contaminated with tramp oil that provided a substrate for bacterial growth and tended to upset the operations of the tube reducer machine. The tramp oil also...
Author(s)
Dennis L. BurnsKirby S. Mohr
SourceProceedings of the Water Environment Federation
SubjectSession 6: Waste Minimization and Wastes Recycle/Reuse
Document typeConference Paper
PublisherWater Environment Federation
Print publication date Jan, 2000
ISSN1938-6478
SICI1938-6478(20000101)2000:5L.293;1-
DOI10.2175/193864700785155803
Volume / Issue2000 / 5
Content sourceIndustrial Wastes (IW) Conference
First / last page(s)293 - 299
Copyright2000
Word count201

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Description: Book cover
Coolant Waste Minimization Using a Coalescing Plate Separator
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Description: Book cover
Coolant Waste Minimization Using a Coalescing Plate Separator
Abstract
During 1998 a project was initiated at Wolverine Tube in Shawnee, Oklahoma to increase machine tool coolant life and also to increase the life of the tooling used to manufacture copper tubing from copper billets.The coolant was becoming contaminated with tramp oil that provided a substrate for bacterial growth and tended to upset the operations of the tube reducer machine. The tramp oil also caused undue wear on the tooling and reduced tooling life.An initial test was conducted using a small, relatively low flow rate coalescing plate separator manufactured by Facet International, Inc. This test was very successful, but the flow rate from the test separator was not adequate for the requirements of the tube reducing operations. A larger separator was subsequently constructed and installed. The separator has been in service more than a year.The paper will present the results of the initial testing as well as the longer-term reduction in waste coolant production and tooling/operating cost reduction. Coolant waste is reduced to approximately 1/3 of previous quantities and costs are substantially reduced. The tramp oil removed by the separator is being recycled as well, and information on this recycling will be presented.
During 1998 a project was initiated at Wolverine Tube in Shawnee, Oklahoma to increase machine tool coolant life and also to increase the life of the tooling used to manufacture copper tubing from copper billets.The coolant was becoming contaminated with tramp oil that provided a substrate for bacterial growth and tended to upset the operations of the tube reducer machine. The tramp oil also...
Author(s)
Dennis L. BurnsKirby S. Mohr
SourceProceedings of the Water Environment Federation
SubjectSession 6: Waste Minimization and Wastes Recycle/Reuse
Document typeConference Paper
PublisherWater Environment Federation
Print publication date Jan, 2000
ISSN1938-6478
SICI1938-6478(20000101)2000:5L.293;1-
DOI10.2175/193864700785155803
Volume / Issue2000 / 5
Content sourceIndustrial Wastes (IW) Conference
First / last page(s)293 - 299
Copyright2000
Word count201

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Dennis L. Burns# Kirby S. Mohr. Coolant Waste Minimization Using a Coalescing Plate Separator. Alexandria, VA 22314-1994, USA: Water Environment Federation, 2018. Web. 9 Jul. 2025. <https://www.accesswater.org?id=-287481CITANCHOR>.
Dennis L. Burns# Kirby S. Mohr. Coolant Waste Minimization Using a Coalescing Plate Separator. Alexandria, VA 22314-1994, USA: Water Environment Federation, 2018. Accessed July 9, 2025. https://www.accesswater.org/?id=-287481CITANCHOR.
Dennis L. Burns# Kirby S. Mohr
Coolant Waste Minimization Using a Coalescing Plate Separator
Access Water
Water Environment Federation
December 22, 2018
July 9, 2025
https://www.accesswater.org/?id=-287481CITANCHOR