lastID = -299068
Skip to main content Skip to top navigation Skip to site search
Top of page
  • My citations options
    Web Back (from Web)
    Chicago Back (from Chicago)
    MLA Back (from MLA)
Close action menu

You need to login to use this feature.

Please wait a moment…
Please wait while we update your results...
Please wait a moment...
Description: Access Water
Context Menu
Description: Book cover
A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities
  • Browse
  • Compilations
    • Compilations list
  • Subscriptions
Tools

Related contents

Loading related content

Workflow

No linked records yet

X
  • Current: 2022-05-06 13:08:55 Adam Phillips
  • 2022-05-06 13:08:54 Adam Phillips
  • 2020-03-26 22:56:13 Adam Phillips
  • 2020-03-26 22:56:12 Adam Phillips
  • 2020-01-31 18:47:43 Administrator
  • 2020-01-31 18:47:42 Administrator
Description: Access Water
  • Browse
  • Compilations
  • Subscriptions
Log in
0
Accessibility Options

Base text size -

This is a sample piece of body text
Larger
Smaller
  • Shopping basket (0)
  • Accessibility options
  • Return to previous
Description: Book cover
A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities

A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities

A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities

  • New
  • View
  • Details
  • Reader
  • Default
  • Share
  • Email
  • Facebook
  • Twitter
  • LinkedIn
  • New
  • View
  • Default view
  • Reader view
  • Data view
  • Details

This page cannot be printed from here

Please use the dedicated print option from the 'view' drop down menu located in the blue ribbon in the top, right section of the publication.

screenshot of print menu option

Description: Book cover
A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities
Abstract
The JD Phillips wastewater plant at Colorado Springs Utilities commenced operations in 2008. Designed for the treatment of 20 MGD the actual flow is 8 MGD. The secondary treatment has three passes. The A pass is used for phosphorus removal and partial denitrification. Passes B & C are used for nitrification. The plant wants to insure compliance to its varying discharge permit while reducing costs.Due to high ammonia influent concentration and a deficiency in BOD it was soon apparent that the plant needed improvements: low alkalinity created some pH excursions outside the discharge permit. Also, energy usage was high. In 2009, a source for additional carbon was found and instruments to measure ammonium, nitrate and pH were installed.Multiple phases have already been implemented and further improvements remain possible. A step by step approach changed the way aeration and denitrification are controlled.In the initial phase the measurement of Dissolved Oxygen was used to control the aeration of the B and C passes. The set points were 2.5 mg/l in pass B and 1.8 mg/l in pass C.In a second phase presented at WEFTEC 2010 the DO set point in the B and C passes were driven by the concentration of ammonia. Savings in energy and chemicals related to the addition of whey, partial denitrification and the use of ammonia measurement were reported.In the phase reported now, the B pass air flow is now controlled directly based on ammonia. The internal recirculation is driven by the nitrate concentration in the C pass. The air flow to the C pass is controlled to maintain a minimum dissolved oxygen concentration at the end of the effluent channelAs a result of those changes in control, additional energy savings have been achieved. Close to 20% savings normalized for flow and ammonia load
The JD Phillips wastewater plant at Colorado Springs Utilities commenced operations in 2008. Designed for the treatment of 20 MGD the actual flow is 8 MGD. The secondary treatment has three passes. The A pass is used for phosphorus removal and partial denitrification. Passes B & C are used for nitrification. The plant wants to insure compliance to its varying discharge permit while reducing...
Author(s)
Robert LagrangeJay HardisonBill HoytJim BeaboutMark Hill
SourceProceedings of the Water Environment Federation
SubjectSession 12: Using Automation and Instrumentation to Reduce Energy Consumption
Document typeConference Paper
PublisherWater Environment Federation
Print publication date Jan, 2011
ISSN1938-6478
SICI1938-6478(20110101)2011:6L.746;1-
DOI10.2175/193864711802836913
Volume / Issue2011 / 6
Content sourceEnergy Conference
First / last page(s)746 - 756
Copyright2011
Word count308
Subject keywordsInstrumentationControlEnergynutrients

Purchase price $11.50

Get access
Log in Purchase content Purchase subscription
You may already have access to this content if you have previously purchased this content or have a subscription.
Need to create an account?

You can purchase access to this content but you might want to consider a subscription for a wide variety of items at a substantial discount!

Purchase access to 'A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities'

Add to cart
Purchase a subscription to gain access to 18,000+ Proceeding Papers, 25+ Fact Sheets, 20+ Technical Reports, 50+ magazine articles and select Technical Publications' chapters.
Loading items
There are no items to display at the moment.
Something went wrong trying to load these items.
Description: Book cover
A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities
Pricing
Non-member price: $11.50
Member price:
-299068
Get access
-299068
Log in Purchase content Purchase subscription
You may already have access to this content if you have previously purchased this content or have a subscription.
Need to create an account?

You can purchase access to this content but you might want to consider a subscription for a wide variety of items at a substantial discount!

Purchase access to 'A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities'

Add to cart
Purchase a subscription to gain access to 18,000+ Proceeding Papers, 25+ Fact Sheets, 20+ Technical Reports, 50+ magazine articles and select Technical Publications' chapters.

Details

Description: Book cover
A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities
Abstract
The JD Phillips wastewater plant at Colorado Springs Utilities commenced operations in 2008. Designed for the treatment of 20 MGD the actual flow is 8 MGD. The secondary treatment has three passes. The A pass is used for phosphorus removal and partial denitrification. Passes B & C are used for nitrification. The plant wants to insure compliance to its varying discharge permit while reducing costs.Due to high ammonia influent concentration and a deficiency in BOD it was soon apparent that the plant needed improvements: low alkalinity created some pH excursions outside the discharge permit. Also, energy usage was high. In 2009, a source for additional carbon was found and instruments to measure ammonium, nitrate and pH were installed.Multiple phases have already been implemented and further improvements remain possible. A step by step approach changed the way aeration and denitrification are controlled.In the initial phase the measurement of Dissolved Oxygen was used to control the aeration of the B and C passes. The set points were 2.5 mg/l in pass B and 1.8 mg/l in pass C.In a second phase presented at WEFTEC 2010 the DO set point in the B and C passes were driven by the concentration of ammonia. Savings in energy and chemicals related to the addition of whey, partial denitrification and the use of ammonia measurement were reported.In the phase reported now, the B pass air flow is now controlled directly based on ammonia. The internal recirculation is driven by the nitrate concentration in the C pass. The air flow to the C pass is controlled to maintain a minimum dissolved oxygen concentration at the end of the effluent channelAs a result of those changes in control, additional energy savings have been achieved. Close to 20% savings normalized for flow and ammonia load
The JD Phillips wastewater plant at Colorado Springs Utilities commenced operations in 2008. Designed for the treatment of 20 MGD the actual flow is 8 MGD. The secondary treatment has three passes. The A pass is used for phosphorus removal and partial denitrification. Passes B & C are used for nitrification. The plant wants to insure compliance to its varying discharge permit while reducing...
Author(s)
Robert LagrangeJay HardisonBill HoytJim BeaboutMark Hill
SourceProceedings of the Water Environment Federation
SubjectSession 12: Using Automation and Instrumentation to Reduce Energy Consumption
Document typeConference Paper
PublisherWater Environment Federation
Print publication date Jan, 2011
ISSN1938-6478
SICI1938-6478(20110101)2011:6L.746;1-
DOI10.2175/193864711802836913
Volume / Issue2011 / 6
Content sourceEnergy Conference
First / last page(s)746 - 756
Copyright2011
Word count308
Subject keywordsInstrumentationControlEnergynutrients

Actions, changes & tasks

Outstanding Actions

Add action for paragraph

Current Changes

Add signficant change

Current Tasks

Add risk task

Connect with us

Follow us on Facebook
Follow us on Twitter
Connect to us on LinkedIn
Subscribe on YouTube
Powered by Librios Ltd
Powered by Librios Ltd
Authors
Terms of Use
Policies
Help
Accessibility
Contact us
Copyright © 2024 by the Water Environment Federation
Loading items
There are no items to display at the moment.
Something went wrong trying to load these items.
Description: WWTF Digital Boot 180x150
WWTF Digital (180x150)
Created on Jul 02
Websitehttps:/­/­www.wef.org/­wwtf?utm_medium=WWTF&utm_source=AccessWater&utm_campaign=WWTF
180x150
Robert Lagrange# Jay Hardison# Bill Hoyt# Jim Beabout# Mark Hill. A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities. Alexandria, VA 22314-1994, USA: Water Environment Federation, 2018. Web. 6 Jun. 2025. <https://www.accesswater.org?id=-299068CITANCHOR>.
Robert Lagrange# Jay Hardison# Bill Hoyt# Jim Beabout# Mark Hill. A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities. Alexandria, VA 22314-1994, USA: Water Environment Federation, 2018. Accessed June 6, 2025. https://www.accesswater.org/?id=-299068CITANCHOR.
Robert Lagrange# Jay Hardison# Bill Hoyt# Jim Beabout# Mark Hill
A Change in Control Strategy Reduces Power Consumption at Colorado Springs Utilities
Access Water
Water Environment Federation
December 22, 2018
June 6, 2025
https://www.accesswater.org/?id=-299068CITANCHOR